I found a fantastic writeup on how to do the procedure here: http://www.audizine.com/forum/showthrea ... nstall-DIY.
Most of what's in that writeup is spot-on, but IMHO he could have put a little more emphasis on getting the subframe down far enough... it makes ALL the difference. When we removed the pan, I was using his "pry the subframe down with a 2x4" technique or a variation: I actually used a crowbar. But in practical terms you can only pry one side at a time that way and it's hard to get it down far enough. With my wife's help, we were barely able to get the pan out on Thursday.
Yesterday I was working by myself and had to find another solution, and as it turns out a MUCH better one. Here's a photo:

That's a gear puller, with the arms removed, pushing against a random object I had lying around with a hole in the middle (so the little point on the end of the puller has a place to sit). You crank down the screw on the gear puller and down goes the subframe! I'm fortunate enough to own two gear pullers and used one on each side, and not to pat myself on the back too much but it worked brilliantly. With the subframe down far enough you don't have to deal with that one $#@#$ bolt that is blocked by the subframe but you can't get the pan out without removing it, and you don't have to worry about messing up the bead of RTV on the pan when you reinstall it. If you're going to do this job, I'd highly recommend getting a couple of gear pullers, or maybe threaded rod and nuts and washers to create a setup like this.
When we finally got the pan out, it really wasn't all that bad:

The pickup tube wasn't horribly clogged but definitely wasn't great:

Interestingly, most of what was in it looks to be bits of the RTV they used to seal the oil pan at the factory!
The worst part was when I realized the pickup tube I was going to use as a replacement, that I got from ECS, was the wrong part. So instead I got to clean this one and reinstall it... that took a while (including a long time soaking it in different solvents) but I think I got 90% of the guck out.
Other than that I did the motor-flush thing then changed the oil again, but I didn't get a chance to do another leakdown test to see what effect there was. Hopefully sometime in the next few weeks I'll be able to do that. I will say that with the motor flush, the oil that came out of the engine was a LOT darker in color than when I put it in 5 minutes earlier!

